Accident Cessna 172M Skyhawk N73115, Wednesday 25 July 2012
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Date:Wednesday 25 July 2012
Type:Silhouette image of generic C172 model; specific model in this crash may look slightly different    
Cessna 172M Skyhawk
Registration: N73115
MSN: 17267271
Year of manufacture:1976
Engine model:Lycoming O-320-E2D
Fatalities:Fatalities: 1 / Occupants: 1
Other fatalities:0
Aircraft damage: Substantial
Location:San Juan Bay, Miramar, San Juan -   Puerto Rico
Phase: Approach
Departure airport:Arecibo, PR (TJAB)
Destination airport:San Juan, PR (TJIG)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
About 4 minutes before the accident, the pilot advised an air traffic controller that an aileron cable had broken but that he was continuing to the airport to land. Security video and eyewitness reports revealed that the airplane was at low altitude and appeared to be maintaining level flight until it banked right, descended, and impacted water near the airport in a right-wing-down attitude.
A postaccident examination of the wreckage indicated that all of the airplane’s flight control cables were lubricated except for a fractured section of aileron control direct cable near the doorpost pulley, which was likely not properly lubricated. Most of the cable strands and the doorpost pulley and bearing exhibited severe corrosion near the fracture. When manipulated by hand, the pulley bearing would not rotate due to the corrosion. Analysis of the cable, doorpost pulley, and an exemplar cable from a similar make and model aircraft that had been flown in similar atmospheric conditions (in what is considered a severe corrosion zone) revealed moderate to severe corrosion. It is likely that, during the airplane’s maintenance inspection 6 months before the accident, the mechanic failed to detect the corroded cable due to the difficulty in visually seeing the cable. It is also likely that the doorpost pulley’s failure to rotate resulted in tension on the right aileron control cable, which subsequently caused it to fail due to the severe corrosion. The aircraft manufacturer’s maintenance manual for the airplane gives specific instructions for lubricating and inspecting flight control cables and pulleys every 600 hours or 12 months, whichever comes first, including, in part, examining the cables for corrosion and the pulleys to ensure smooth rotation. After the accident, the manufacturer produced a video emphasizing the importance of properly examining and lubricating the cables.

Probable Cause: Maintenance personnel’s improper lubrication of the right direct aileron control cable and failure to detect the severe corrosion of the cable during a maintenance inspection, which resulted in the in-flight failure of the cable, the pilot’s subsequent inability to maintain aircraft control, and the airplane’s impact with terrain.




Revision history:

26-Jul-2012 02:09 AngelS360 Added
26-Jul-2012 02:12 harro Updated [Source, Narrative]
26-Jul-2012 17:41 Geno Updated [Location, Source]
28-Jul-2012 12:26 Alpine Flight Updated [Aircraft type, Operator]
02-Aug-2012 18:31 Geno Updated [Time, Source, Narrative]
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
27-Nov-2017 20:55 ASN Update Bot Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative]

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