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Date: | Sunday 5 March 2023 |
Time: | 18:09 |
Type: | Honda HA-420 HondaJet Elite |
Owner/operator: | Nesama LLC dba Volato |
Registration: | N118CX |
MSN: | 42000231 |
Year of manufacture: | 2022 |
Total airframe hrs: | 486 hours |
Engine model: | General Electric HF-120 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Other fatalities: | 0 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Buena Vista-Central Colorado Regional Airport (AEJ/KAEJ), CO -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Monterey Regional Airport, CA (MRY/KMRY) |
Destination airport: | Buena Vista-Central Colorado Regional Airport, CO (KAEJ) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane was coming into the airport to land following a cross-country flight. The pilot reported they checked the weather, entered the current conditions in the Garmin Control Unit, and received the results they expected for the RNAV approach to runway 33. The airport manager came on the radios and reported the winds as 280o at 8 knots, gusting to 19 knots. The crew captured the glidepath before the final approach fix and the co-pilot called out speeds to touchdown, the last being 115 kts. The touchdown was normal, but then the airplane experienced a strong yaw to the left from a wind gust. The pilot attempted to steer the airplane back, but the airplane went off the left side of the runway, struck a taxiway sign, and came to a stop with the nose of the airplane facing the runway. The airplane sustained substantial damage to the left inboard wing and lower left fuselage. The crew reported no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operation.
At the time of the accident, the airplane was landing on runway 33 with reported winds 280o at 8 knots with gusts to 24 knots.
Following the accident, the company put in place stricter crosswind component limits for its’ fleet of airplanes.
Probable Cause: The pilot’s inability to maintain directional control during landing with a gusting left crosswind resulting in the runway excursion.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN23LA134 |
Status: | Investigation completed |
Duration: | 5 months |
Download report: | Final report |
|
Sources:
NTSB
https://data.ntsb.gov/Docket?ProjectID=106886 https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=118CX https://globe.adsbexchange.com/?icao=a04a33&lat=38.792&lon=-106.137&zoom=14.0&showTrace=2023-03-06&leg=1×tamp=1678065296
https://flightaware.com/live/flight/N118CX https://www.flightradar24.com/data/aircraft/n118cx#2f6b9a19 https://flyvolato.com/wp-content/uploads/2022/11/honda-jet.png.webp (photo)
Location
Images:
Revision history:
Date/time | Contributor | Updates |
31-Aug-2023 18:50 |
Captain Adam |
Updated |
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