Accident de Havilland Canada DHC-8-106 TF-JMB, Friday 4 March 2011
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Date:Friday 4 March 2011
Type:Silhouette image of generic DH8A model; specific model in this crash may look slightly different    
de Havilland Canada DHC-8-106
Owner/operator:Flugfélag Íslands - Air Iceland
Registration: TF-JMB
MSN: 337
Year of manufacture:1992
Total airframe hrs:32336 hours
Cycles:35300 flights
Engine model:Pratt & Whitney Canada PW121
Fatalities:Fatalities: 0 / Occupants: 34
Other fatalities:0
Aircraft damage: Substantial, written off
Location:Nuuk Airport (GOH) -   Greenland
Phase: Landing
Nature:Passenger - Scheduled
Departure airport:Kulusuk Airport (KUS/BGKK)
Destination airport:Nuuk Airport (GOH/BGGH)
Investigating agency: HCLJ
Confidence Rating: Accident investigation report completed and information captured
A DHC-8 passenger plane, registered TF-JMB, sustained substantial damage in a landing accident at Godthåb/Nuuk Airport (GOH), Greenland. All 31 passengers and three crew members survived. The airplane operated on a flight from Reykjavík Domestic Airport (RKV), Iceland to Godthåb/Nuuk Airport (GOH), Greenland with an enroute stop at Kulusuk.
At 12:58, the flight crew of TF-JMB made radio contact with Nuuk AFIS and were informed that the runway in use was 23.
The weather was reported to be: wind direction from 170° at a speed of 24 kts with a maximum of 43 kts, the visibility was 4,000 meters in light snow, moderate blowing snow, a few clouds at 1,800 feet, broken clouds at 3,500 feet, the temperature was zero, the dew point was minus four Celsius and the QNH was 1014 hPa.
The flight crew made visual contact with the runway and decided to deviate to the right (west) of the offset Localizer (LLZ) to runway 23. The flight continued towards the runway from a position right of the runway centerline. The flight crew was aiming to land the aircraft at a point between the runway threshold and the touchdown zone.
As the aircraft approached runway 23 it was still in the final right turn over the landing threshold.
The aircraft touched down on runway 23 between the runway threshold and the touchdown zone and to the left of the runway centerline. The Flight Data Recorder (FDR) data indicated that the aircraft was banking more than 11° to the right as the aircraft touched down. At the same time the vertical acceleration was approximately 3.9 G and the rate of descent was greater than 13 feet per second.
The right main landing gear (MLG) shock strut fuse pin sheared and the right MLG collapsed, the aircraft skidded down the runway and departed the runway to the right.
The nose landing gear was separated from the aircraft as the aircraft was entering the unpaved surface. The aircraft came to rest in the rocky area to the right of runway 23.

Adverse wind and turbulence conditions at BGGH led to flight crew task saturation on final approach and a breakdown of optimum cockpit resource management (CRM) resulting in a divergence from the operator’s stabilized approach policy.
The divergence from the operator’s stabilized approach policy caused an unstabilized approach and a hard landing leading to an excess load of the right MLG at touchdown.
According to its design, the right MLG fuse pin sheared as a result of stress

Accident investigation:
Investigating agency: HCLJ
Report number: HCLJ510-000828
Status: Investigation completed
Duration: 2 years and 5 months
Download report: Final report


Sermitsiaq (4-3-2011) (4-3-2011)



photo (c) David Booster; Reykjavík Domestic Airport (RKV/BIRK); 01 June 2010

photo (c) Tomas Milosch; Godthåb/Nuuk Airport (GOH/BGGH); 03 June 2010

Revision history:


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