Date: | Monday 6 December 2004 |
Time: | 13:29 |
Type: | Gulfstream G-IV |
Owner/operator: | Centurion Aviation Services |
Registration: | N478GS |
MSN: | 1478 |
Year of manufacture: | 2002 |
Total airframe hrs: | 2004 hours |
Engine model: | Rolls-Royce Tay 611-8 |
Fatalities: | Fatalities: 0 / Occupants: |
Other fatalities: | 0 |
Aircraft damage: | Substantial, repaired |
Category: | Accident |
Location: | Bucharest Baneasa Aurel Vlaicu International Airport (BBU) -
Romania
|
Phase: | Landing |
Nature: | Passenger - Non-Scheduled/charter/Air Taxi |
Departure airport: | Bagram Air Base (OAI/OAIX) |
Destination airport: | Bucharest Baneasa Aurel Vlaicu International Airport (BBU/LRBS) |
Investigating agency: | CIAS |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The Gulfstream G-IV suffered a runway excursion after landing on runway 07 at Bucharest Baneasa Airport.
On the day of the accident maintenance works were being carried out on runway 07 with the partial removal and replacement of concrete. The threshold was displaced, causing landing distance available to become 2360 m.
The G-IV landed long and fast and could not be stopped on the runway. It overshot the runway threshold and taxied with the left main leg on an unpaved section with a depth of approx. 15-20 cm, and came to rest on the edge of the runway. The crew reported massive fuel leakage from the left wing.
As a result, the aircraft sustained damage to the left main landing gear strut and the fuel tank in the left wing.
Causes of the accident
Contributory factors :
- Performing the approach procedure at high approach speed since entering TMA Bucuresti; ,
- Unstabilized approach at high speed on the ILS slope;
- Continuation of ILS approach under conditions of not properly intercepting the slope;
- Failure to initiate the missed procedure when EGPWS signals appeared (during the instrument landing at 100 ft, it is assumed that the aircraft was on the landing slope, with the checklist completed) ;
- "Long" landing of the aircraft (about 1000 M from the threshold of runway 07) and at high speed - indicated in the plot (195 Kts at 0.5 NM from threshold and 179 Kts at touchdown);
- delay of brake actuation as well as delay of thrust reverser operation after actuation.
Contributing :
- Long landing with overshoot of available landing area.
Accident investigation:
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| |
Investigating agency: | CIAS |
Report number: | Nr.31 |
Status: | Investigation completed |
Duration: | 2 years and 2 months |
Download report: | Final report |
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Sources:
Revision history:
Date/time | Contributor | Updates |
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