Accident Beechcraft A36 Bonanza N36900, Thursday 20 July 2023
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Date:Thursday 20 July 2023
Time:12:36
Type:Silhouette image of generic BE36 model; specific model in this crash may look slightly different    
Beechcraft A36 Bonanza
Owner/operator:Private
Registration: N36900
MSN: E-1739
Year of manufacture:1980
Fatalities:Fatalities: 0 / Occupants: 2
Other fatalities:0
Aircraft damage: Substantial
Category:Accident
Location:near Oberlin, KS -   United States of America
Phase: En route
Nature:Private
Departure airport:Gillette-Campbell County Airport, WY (GCC/KGCC)
Destination airport:Dalhart Airport, TX (DHT/KDHT)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that while in cruise flight over a cloud layer, the engine lost power as if it were out of fuel. The pilot attempted to restore engine power by switching to the right fuel tank and activating the starter but was unsuccessful. As the airplane descended through the cloud layer, the pilot switched back to the left fuel tank and then focused his attention on maintaining airplane control. The airplane descended below the cloud layer and the pilot maneuvered the airplane for a forced landing to a road. During the forced landing, the airplane impacted terrain, resulting in substantial damage to the left wing and fuselage.

Examination of the fuel system revealed that the fuel venting system on the left-wing fuel tank was obstructed by what appeared to be insect debris. No other anomalies were noted during the examination of the airframe and engine that would have precluded normal operations.

The circumstances of the power loss are consistent with an interruption of fuel flow from the left fuel tank due to inadequate venting of the fuel tank.

During the attempt to restore engine power, the pilot did not engage the auxiliary fuel pump as stated in the emergency procedures checklist, which may have aided in restoring engine power.

Probable Cause: The blockage of the left fuel tank vent, which resulted in a total loss of engine power due to fuel starvation. Contributing to the accident of the pilot’s failure to use his checklist to address the loss of engine power.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN23LA344
Status: Investigation completed
Duration: 9 months
Download report: Final report

Sources:

NTSB

https://data.ntsb.gov/Docket?ProjectID=192781
https://flightaware.com/live/flight/N36900

Location

Images:


Photo: NTSB

Revision history:

Date/timeContributorUpdates
15-Aug-2023 19:40 Captain Adam Added
16-May-2024 07:42 Captain Adam Updated [Source, Narrative, Photo]

Corrections or additions? ... Edit this accident description

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