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Date: | Tuesday 20 January 1998 |
Time: | 09:25 LT |
Type: | Cessna 208B Super Cargomaster |
Owner/operator: | Baron Aviation Services |
Registration: | N738FX |
MSN: | 208B0482 |
Year of manufacture: | 1995 |
Total airframe hrs: | 1139 hours |
Engine model: | P&W PT-6A-114A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Other fatalities: | 0 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Grand Island, NE -
United States of America
|
Phase: | Landing |
Nature: | Unknown |
Departure airport: | Omaha, NE (KOMA) |
Destination airport: | (KGRI) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was in cruise flight at 4,000 feet mean sea level (msl), when moderate ice began forming on the airplane. The pilot requested and received approval from air traffic control to climb to a higher altitude. The airplane reached an altitude of 6,700 feet msl, and would not climb any higher. The pilot maintained 6,500 feet msl until he turned onto the VOR/DME approach for runway 31 at Grand Island. The pilot maintained an airspeed between 125 and 140 knots on the approach. When the airplane was over the runway, the pilot reduced the throttle from cruise power. The airplane began to drop. The pilot said that he added power, but it did not stop the sink rate. The airplane touched down hard on the runway, slowly veered to the left, departed the runway, and turned around 180 degrees in a field before coming to a stop. Approximately 1-1/2 inches of clear ice was observed adhering to the leading edges of the wings and empennage after the accident.
Probable Cause: ice build-up on the airplane's wings and empennage which led to an inadvertent stall and hard landing. Factors contributing to this accident were the pilot's inadvertent flight into icing conditions, and the icing conditions.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI98LA084 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB CHI98LA084
History of this aircraft
Other occurrences involving this aircraft
27 April 2004 |
N738FX |
Baron Aviation |
0 |
19 km NE of Helena, AR |
|
sub |
Forced landing |
25 September 2013 |
C-FEXV |
Morningstar Air Express |
1 |
Hudson Bay, ON |
|
w/o |
Revision history:
Date/time | Contributor | Updates |
11-Mar-2024 19:11 |
ASN Update Bot |
Added |
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