This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 25 March 1987 |
Time: | 09:30 LT |
Type: | McDonnell Douglas DC-10-10 |
Owner/operator: | American Airlines |
Registration: | N128AA |
MSN: | 46984/250 |
Total airframe hrs: | 29020 hours |
Engine model: | GE CF6-6K |
Fatalities: | Fatalities: 0 / Occupants: 177 |
Other fatalities: | 0 |
Aircraft damage: | None |
Category: | Accident |
Location: | Chicago, IL -
United States of America
|
Phase: | Initial climb |
Nature: | Passenger - Scheduled |
Departure airport: | Chicago, IL (KORD) |
Destination airport: | Dallas/Fort Worth International Airport, TX (DFW/KDFW) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:AFTER ARRIVING AT THE GATE IN CHICAGO, FUMES & SMOKE WERE NOTED IN ZONE C OF THE CABIN, THEN THE CABIN LGTG WENT OUT & THE EMERG LGTG CAME ON. MAINT PSNL FND THE #2 APU HAD AN AUTO-SHUTDOWN DUE TO A MALFUNCTION. THE APU WAS PLACARDED AS INOP & THE ACFT WAS RTRND TO SVC. AS IT WAS CLBG, SHORTLY AFTER TAKEOFF, SMOKE BCM NOTICEABLE & THE CREW ELECTED TO RTRNTO THE ARPT & LND. AFTER LNDG, THE SMOKE HAD DISSIPATED & FIRE DEPT PSNL RPRTD NO INDCN OF SMOKE OR FIRE. SUSPECTING ONLY AN AIR CONDITIONING PROBLEM, THE CREW ELECTED TO CONT TO THE GATE. AS THEY BGN TAXIING, A FLT ATTENDANT RPRTD THE SMOKE WAS INCREASING, SO THE CAPT STOPPED THE ACFT & DIRECTED AN EVACUATION. A X-WIND PREVENTED PROPER DEPLOYMENT OF THESLIDES ON THE RGT SIDE OF THE ACFT. DRG THE EVACUATION, AN ELDERLY PAX, USING SLIDE L-4 ON THE LEFT SIDE, WAS SERIOUSLY INJURED BY OTHERS WHO CAME DOWN THE SLIDE AFTER HIM. ALSO, 5 PAX RECEIVED MINOR INJURIES DRG EVACUATION. AN INV REVEALEDTHE SMOKE WAS CAUSED BY OIL FROM A FAILED APU BEARING WHICH LEAKED INTO THE AIR CONDITIONING SYS.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI87MA101 |
Status: | Investigation completed |
Duration: | 1 year and 7 months |
Download report: | Final report |
|
Sources:
NTSB CHI87MA101
Revision history:
Date/time | Contributor | Updates |
27-Mar-2024 12:26 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation